There are 6 owner-reported engine complaints for the 2007 Ford F-250in NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
See attached document for complaint
EGL COOLER FAILURE, WHITE SMOKE COMING OUT OF THE EXHAUST PIPE CAUSED BY COOLANT ENTERING INTO THE EMISSION SYSTEM. "ON ALL 6.0 ENGINES THE EGL COOLER WILL FAIL." THIS PROBLEM IS SO "MASSIVE" WITH SO MANY "MASSIVE COMPLAINTS FROM CUSTOMERS" THAT FORD HAS DONE TWO THINGS 1) DESIGNED A BY-PASS KIT AND 2) RE-DESIGNED THE ENGINE TO ELIMINATE THE PROBLEM (6.7 ENGINE). WHEN THE EGL COOLER FAILS, FORD OFFERS TWO SOLUTIONS TO THE CUSTOMER 1) INSTALL THE BY-PASS KIT AND THE PROBLEM IS SOLVED (AT A COST OF $4500) OR 2) REPAIR THE EGL COOLER TO BRING IT "BACK TO FACTORY" (AT A COST OF $4300). FORD TELLS CUSTOMERS THAT IF OPTION 2 IS CHOSEN, THE "EGL COOLER WILL FAIL AGAIN". ALL QUOTES USED ARE DIRECT QUOTES FROM FORD'S SERVICE DEPARTMENT. *TR
TL* THE CONTACT OWNS A 2007 FORD F250. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 40 MPH, WHITE SMOKE EMITTED FROM THE EXHAUST AS THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TOWED TO A DEALER, WHO STATED THAT THE OIL COOLER WAS DEFECTIVE AND THE ERG VALVE WOULD NEED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE WAS 37,188.
TL* THE CONTACT OWNS A 2007 FORD F-250. THE CONTACT STATED THAT THE HEAD GASKET MALFUNCTIONED, CAUSING COOLANT TO SPRAY OVER THE ENGINE. THE CONTACT TOOK THE VEHICLE TO THE DEALER TO HAVE THE HEAD GASKET REPLACED. THE CONTACT CALLED THE MANUFACTURER REGARDING THE HEAD GASKET AND THE MANUFACTURER ADVISED THAT THE HEAD GASKET WAS BLOWN DUE TO A DESIGN FLAW. THE FAILURE MILEAGE WAS 88,000.
THE TRUCK I AM PAYING OVER $50,000 FOR HAS LEFT ME STRANDED AND HAS BEEN TOWED 3 TIMES IN THE LAST MONTH. PURCHASED END OF JAN. '07, HAS 30,000 MILES WITH A DIESEL ENGINE. I AM AFRAID TO TAKE THIS TRUCK BACK ON THE ROAD AND FORD SAYS ALL THEY ARE OBLIGATED TO DO IS REPAIR THE TRUCK. THIS IS THE 4TH ATTEMPT. *TR
ELECTRONIC THROTTLE CONTROL (DRIVE BY WIRE) FAILS INTERMITTENTLY. ENGINE GOES TO IDLE WITH ABSOLUTELY NO RESPONSE TO THE THROTTLE PEDAL WHILE DRIVING. PEDAL ASSEMBLY HAS BEEN REPLACED TWICE AND THE PCM ONCE. VEHICLE HAS LESS THAN 1500 MILES. *NM
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 26, 2026