There are 26 owner-reported engine complaints for the 2015 Ford Transitin NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
The contact owns a 2015 Ford Transit. The contact stated that while his brother was driving at an undisclosed speed, the check engine warning light illuminated. The vehicle was taken to an independent mechanic, where it was diagnosed, and it was determined that the fuel pump module needed to be replaced. The vehicle was not repaired. The manufacturer was notified of the failure. The failure mileage was approximately 100,000.
The contact owns a 2015 Ford Transit. The contact stated while driving at an undisclosed speed, the message "Exhaust filter overloaded, drive to clean", after which the vehicle entered LIMP Mode, and was unable to accelerate above 30 MPH. The check engine warning light was illuminated. The vehicle was taken to the dealer, who diagnosed a failure with the Diesel Particulate Filter (DPF). The vehicle was repaired under Customer Satisfaction Program: 23M01, but the failure reoccurred. The vehicle was then taken to an independent mechanic, who diagnosed a failure with the Diesel Particulate Filter (DPF). The vehicle was not repaired. The manufacturer was notified of the failure, and a case was opened. The failure mileage was 109,000.
The contact owns a 2015 Ford Transit. The contact stated that while at a stop light, the vehicle stalled. The vehicle was towed to the local dealer to be diagnosed. The contact was informed that the engine had seized and needed to be replaced. The cause of the engine failure was not yet determined. The manufacturer was notified of the failure, but no assistance was offered. The failure mileage was 59,000.
The contact owns a 2015 Ford Transit. The contact stated while driving at undisclosed speeds, the check engine warning light was illuminated. The contact stated that the failure was related to Customer Satisfaction Program: 15B39 CPR and Technical Service Bulletin: 19-2091. The vehicle was taken to the local dealer, where it was diagnosed with water intrusion from insufficient sealing in certain areas of the engine compartment, allowing water entry into the engine compartment. The vehicle was not repaired. The manufacturer was contacted and confirmed that there was no warranty coverage on vehicle. The failure mileage was approximately 13,000.
See attached document for complaint.
Hi, I’ve been getting water into my engine air filter box. I did some research and a lot of customers are having the same problem. Is there a fix for this..
Warped exhaust manifolds
The 2015 Ford Transit was designed such that rainwater from the windshield drains into the engine and sometimes floods the air filter system. This issue is documented in this NTSA TSB where it's stated: To resolve this condition, install updated water management hardware and/or a revised air cleaner cover. https://static.nhtsa.gov/odi/tsbs/2019/MC-10156525-0001.pdf We were driving along an interstate and were on a long viaduct while it was raining. The engine stalled and we were lucky enough that the vehicle was able to reach the end of the viaduct. I had my spouse and 7 children in the van. We received a tow but myself and 2 children were forced to walk along the interstate as the tow couldn't hold all of us. As this is a large passenger van, it's my opinion as a licensed professional engineer that it poses an substantial fatality risk to occupants because the likelihood of fatalities on interstates is tremendous due to traveling speed. Ford designed a windshield that puts water into the air system which creates a known safety and 100% preventable condition. This should be a factory safety recall repaired in all Ford Transits. Most of these vans are used by government agencies for employee or prison transport or by church/community service groups and has a high percentage of mass casualty or PDO when the system fails. There are multiple YouTube and Ford Transit auto forums highlighting this safety design flaw so it is a well known and attributable problem created by substandard Ford engineering.
Exhaust manifold faulty
Exhaust manifold faulty
Exhaust manifold studs failed and exhaust both manifolds warped at appropriately 85,000 miles. The repair estimate is over $4,000.00.
TL* THE CONTACT OWNS A 2015 FORD TRANSIT. THE CONTACT STATED THAT THE VEHICLE WAS TAKEN FOR SERVICE UNDER NHTSA CAMPAIGN NUMBER: 19V767000 (POWER TRAIN) TO LEITH FORD (5300 ROLESVILLE RD, WENDELL, NC 27591). THE CONTACT STATED THAT THE REPAIR FAILED TO CORRECT THE ISSUE. THE CONTACT STATED THAT WHILE DRIVING, THE VEHICLE WAS MAKING A GROWLING SOUND AND VIBRATED VIOLENTLY. THE CONTACT STATED THAT THE VEHICLE WAS UNSAFE TO DRIVE. THE CONTACT CALLED THE SAME DEALER AND INFORMED THEM OF THE FAILURE. THE DEALER INFORMED THE CONTACT THAT THEY WOULD HAVE TO CHARGE FOR A NEW DIAGNOSTIC TEST TO BE PERFORMED. THE VEHICLE WAS NOT YET TAKEN TO THE DEALER. THE CONTACT MENTIONED THAT THE VEHICLE WAS TAKEN THREE TIME TO THE SAME DEALER FOR THE SAME REPAIRS. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND PROVIDED A CASE NUMBER. THE FAILURE MILEAGE WAS APPROXIMATELY 116,800.
WAS DRIVING TO NEW ORLEANS WHEN I WAS CAUGHT IN A VERY HEAVY RAIN STORM. THE VAN STARTED TO DRIVE ROUGH A DAY LATER. TOOK IT INTO A FORD DEALERSHIP FOR A DRIVESHAFT RECALL AND OIL CHANGE ONLY TO BE TOLD THAT WATER GOT INTO THE HOUSING FOR THE AIR FILTER AND SOAKED THE FILTER. THE WATER THEN MADE IT'S WAY THROUGHOUT THE ENGINE. AFTER, I THEN LEARNED OF FORD ISSUING A TSB THAT WOULD HAVE SAVED MY VAN SHOULD IT OF BEEN A RECALL OR CHECKED BY MY LOCAL FORD DEALERSHIP WHEN I HAD PREVIOUS WORK COMPLETED.
TL* THE CONTACT OWNS A 2015 FORD TRANSIT. THE CONTACT STATED WHILE DRIVING 5 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT PUSHED THE VEHICLE TO A NEARBY PARKING LOT. THE VEHICLE WAS THEN TOWED TO AN INDEPENDENT MECHANIC TO BE DIAGNOSED. THE CONTACT WAS INFORMED THAT THE FUEL RAIL ASSEMBLY, FILTER AND RETURN LINES NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED HOWEVER, THE FAILURE RECURRED AFTER 600 MILES WITH THE REDUCED POWER WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TOWED TO GARY CROSSLEY FORD LOCATED AT (8050 N CHURCH RD, KANSAS CITY, MO 64158), TO BE DIAGNOSED. THE CONTACT WAS INFORMED THAT THE FUEL PUMP, FUEL PUMP AND LOW PRESSURE FUEL SENSOR NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED HOWEVER, THE FAILURE RECURRED. THE CONTACT RESTARTED THE VEHICLE AND DROVE THE VEHICLE BACK TO THE DEALER. THE CONTACT WAS INFORMED BY THE MECHANIC THAT THERE WAS METAL BITS INSIDE THE FUEL SYSTEM AND THE FUEL INJECTOR NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE CONTACT REFERENCED NHTSA CAMPAIGN NUMBER: 16V618000 (FUEL SYSTEM, DIESEL, ENGINE AND ENGINE COOLING) AS A POSSIBLE CAUSE OF THE FAILURE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 56,826.*DT*JB
TL* THE CONTACT OWNS A 2015 FORD TRANSIT 350. THE CONTACT STATED THAT THE AIR INTAKE WAS MOUNTED ON THE VEHICLE IN A WAY THAT ALLOWED WATER TO GET INSIDE AND RUST OUT THE BOLTS THAT SECURED THE AIR INTAKE IN PLACE. AS A RESULT, ANTI-FREEZE WOULD LEAK AND POSSIBLY CAUSE A FIRE. THE VEHICLE WAS LOSING ANTI-FREEZE AND THE TOP OF THE ENGINE WAS SMOKING WHILE THE VEHICLE WAS IN MOTION. THE BOLTS HAD COMPLETELY RUSTED AND THE WATER FROZE WHEN THE VEHICLE WAS PARKED. WHEN THE ICE MELTED AND THE ENGINE WARMED UP FROM DRIVING, A FIRE NEARLY OCCURRED. THE CONTACT SAW SMOKE, PULLED OVER, AND OPENED THE HOOD. THE CONTACT HAD TO CALL TO HAVE MORE ANTI-FREEZE DELIVERED TO REFILL THE VEHICLE. THE VEHICLE WAS TAKEN TO GARNET FORD (1610 WILMINGTON PIKE, WEST CHESTER, PA 19382 (610) 358-5600) WHERE IT WAS IN THE PROCESS OF BEING DIAGNOSED. THE MANUFACTURER WAS CALLED AND TRANSFERRED THE CONTACT TO NHTSA. THE FAILURE MILEAGE WAS 122,000.
THE VEHICLE STALLED UPON BACKING OUT OF A STEEP DRIVEWAY & TURNING TO THE LEFT. IT WOULD NOT RESTART. THE VAN HAD BEEN PARKED, AT A CUSTOMERS' HOME ALL DAY. HEAVY SNOW BEGAN FALLING A COUPLE OF HOURS BEFORE THE VAN WAS STARTED & WARMED UP TO MELT THE SNOW FROM THE WINDSHIELD. WHEN THE VAN STALLED, IT WAS BROADSIDE TO THE STREET, BLOCKING BOTH OPPOSING LANES OF TRAVEL AS THE HEAVY SNOW INCREASED IN INTENSITY. THE VAN WAS VIRTUALLY IMPOSSIBLE TO PUSH OFF TO THE SIDE OF THE ROAD, DUE TO THE QUICKLY ACCUMULATING SNOW, INITIALLY PREVENTING A PLOW & POLICE CRUISER FROM PASSING. AAA TOWING WAS CALLED BUT, DID NOT ARRIVE UNTIL 2 HOURS AFTER BEING SUMMONSED AS THE SNOW CONTINUED TO ACCUMMULATE. I HAD THE VAN TOWED TO OUR BUSINESS LOCATION AND DECIDED TO CHECK THE ENGINE AIR FILTER. WHEN I OPENED THE FILTER HOUSING, IT AND THE AIR FITER WERE WATER-SOAKED. I OBSERVED WATER RUNNING DOWN THE WINDSHIELD, DOWN ALONG THE FIREWALL AND ONTO/INTO THE AIR FILTER BOX. I CONTACTED MY LOCAL FORD DEALER (FORD OF WILBRAHAM, MA, TEL.: 413-543-2800) TO REPORT MY FINDINGS & TO MAKE AN APPOINTMENT TO REMEDY THE PROBLEM. THE SOLUTION WAS PERFORMED AS PER TSB (TECHNICAL SERVICE BULLETIN) #19-2091 AND AT A COST OF $488.45 (INVOICE #659506), WHICH I RELUCTANTLY PAID TO THE DEALER. I EXPLAINED THAT THIS A POOR DESIGN ALLOWING WATER TO RUN DIRECTLY INTO THE AIR FILTER BOX, WHICH, IN TURN, SHUTS DOWN THE ENGINE & RENDERS THE VEHICLE MOTIONLESS & CAN BE DANGEROUS, DEPENDING UPON WHERE & WHEN THE VEHICLES' ENGINE STALLS & THEN FAILS TO RESTART. THE SERVICE WRITER SAID THAT THERE WAS NOTHING SHE COULD DO TO HELP ME & THAT I AM STILL RESPONSIBLE FOR THE COST OF THE TSB. IN ADDITION, MY INVOICE INDICATES THAT RECALL #19S38 WAS PERFORMED, YET IT IS STILL OUTSTANDING ON THE RECALL WEBSITE UNDER MY VEHICLES' VIN. FOR THE RECORD, THIS VAN HAD ONLY 31,853 MILES ON IT, WHEN I BROUGHT IT IN FOR THIS PROBLEM.
IT APPEARS THAT THIS MODEL HAS AN ENGINE FAILURE ISSUE RELATED TO WATER ENTERING THE AIR BOX AND CAUSING THE WATER TO TRAVEL TO COMPONENTS THAT DISABLES THE CAR. I WAS DRIVING IN THE RAIN AND GOT STRANDED ON THE SIDE OF THE INTERSTATE IN HEAVY TRAFFIC AND HEAVY RAIN ON I40 IN KNOXVILLE TN FOR AN HOUR WAITING FOR A TOW TRUCK TO GET ME OUT OF A DANGEROUS SITUATION. HAD IT TOWED TO A DEALER THAT PROCEEDED TO TELL ME THE NEXT DAY THAT THERE WAS A TSB ON THIS ISSUE AND THAT THERE WAS A KIT THAT REMEDIES THE PROBLEM. A DEFLECTOR OF SOME SORT TO KEEP WATER OUT OF THE AIR BOX. THE COST TO THE CONSUMER IS OVER $750 TO GET IT DONE. I STRONGLY BELIEVE THAT IS FORD KNOWS ABOUT ABOUT THIS ISSUE AND HAS COME UP WITH A SOLUTION, IT SHOULD BE A RECALL AND NOT JUST A TSB. THEIR POOR DESIGN AND NEGLIGENCE PUT ME IN A DANGEROUS SITUATION FOR ABOUT AN HOUR . I COULD HAVE BEEN RAMMED BY HIGHWAY TRAVELERS AND POSSIBLY KILLED BECAUSE MY VEHICLE WAS DISABLED BECAUSE OF A POOR DESIGN THAT FORD REFUSES TO REPAIR AT THEIR COST. SOMEONE PLEASE ADVISE FORD AND THEIR DEALERS THAT THIS IS NOT A CONVENIENCE ISSUE, BUT A LIFE THREATENING ISSUE THAT FORD SHOULD ISSUE A RECALL TO REMEDY THE POOR DESIGN AT THEIR COST. THANK YOU.
TL* THE CONTACT OWNS A 2015 FORD TRANSIT. ON SEVERAL OCCASIONS, WHILE DRIVING APPROXIMATELY 10-80 MPH, THE ENGINE FAULT WARNING INDICATOR ILLUMINATED AND THE VEHICLE LOST POWER. THE CONTACT WAS ABLE TO EXIT THE ROADWAY. WHEN THE VEHICLE WAS TURNED OFF AND RESTARTED, IT RESUMED NORMAL OPERATION. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. BARBEE'S FREEWAY FORD (4471 EAST EVANS AVENUE, DENVER, CO, (303) 584-6600) WAS CALLED, BUT WAS UNABLE TO DETERMINE THE CAUSE OF THE FAILURE. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 95,000.
TL* THE CONTACT OWNS A 2015 FORD TRANSIT. THE CONTACT DETECTED AN ABNORMAL EXHAUST OR CARBON MONOXIDE ODOR COMING FROM THE VEHICLE. THE CONTACT TOOK THE VEHICLE TO CLASSIC FORD (8540 TYLER BLVD, MENTOR, OH 44060, (440) 266-3000) WHERE IT WAS DIAGNOSED THAT THE ENGINE BOLTS WERE FRACTURED AND NOT CONNECTED TO THE VEHICLE. THE BOLTS WERE STUCK IN THE ENGINE AND CAUSED A CARBON MONOXIDE LEAK. THE DEALER STATED THAT A NEW ENGINE NEEDED TO BE INSTALLED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 188,000.
ENGINE WOULD STALL WHILE DRIVING AND DOESN'T WANT TO START THIS HAPPENED THREE TIMES ONCE WHILE DRIVING. THIRD TIME IT HAD TO TOWED AWAY . LOOKS LIKE FUEL NOT GETTING TO THE ENGINE OR PROBLEM WITH FUEL SYSTEM
Showing 1–20 of 26 complaints
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 26, 2026