There are 5 owner-reported electrical system complaints for the 2008 Mercury Milanin NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
The contact owns a 2008 Mercury Milan. The contact stated that the speedometer would intermittently fluctuate while driving at various speeds without warning. Despite the speedometer failure, the vehicle would resume normal driving operation. Recently, the contact stated that the failure would occur each time while operating the vehicle. The contact had taken the vehicle to an independent mechanic who stated that the failure could be related to the speed sensor or the computer. The contact then took the vehicle to a dealer who informed him that the failure could be related to a module inside the instrument cluster. The contact had also taken the vehicle to FleetSide Ford, LLC. (1120 Jeffreys Dr, Osceola, IA 50213) where they informed him that they had never heard of such failure. The manufacturer was notified of the failure and informed him that they had never heard of such a failure. No further assistance was provided. The vehicle had yet to be repaired. The failure mileage was 163,188
I WAS DRIVING ABOUT 45 MPH ON A CITY STREET, WHEN THE CAR JUST SHUT DOWN. I TRIED TO GIVE IT GAS, NOTHING HAPPENED. STEERING WHEEL LOCKED UP. I STILL HAD POWER TO THE RADIO AND LIGHTS BUT THE CAR WENT LIMP. I WAS BARLEY ABLE TO TURN IT INTO A PARKING LOT FOR SAFETY BECAUSE THE STEERING WHEEL LOCKED UP. I TURNED OFF THE CAR WAITED A FEW MINUTES AND STARTED IT BACK UP WITH NO PROBLEMS. I AM LUCKY I WASN'T IN TRAFFIC, BECAUSE THIS WOULD HAVE CAUSED AN ACCIDENT, IT WENT FROM 45 MPH TO NOTHING IN SECONDS.
TL* THE CONTACT OWNS A 2008 MERCURY MILAN. THE CONTACT STATED THAT NHTSA CAMPAIGN NUMBER: 17V024000 (AIR BAGS) EXCEEDED A REASONABLE AMOUNT OF TIME FOR REPAIR. THE CONTACT RECEIVED THE RECALL NOTIFICATION IN MARCH OF 2017. THE MANUFACTURER STATED THAT THE PART WAS NOT AVAILABLE FOR REPAIR. THE CONTACT ALSO STATED THAT THE FRONT PASSENGER AIR BAG WAS EXPOSED DUE TO A FRACTURED DASHBOARD AT THE FRONT PASSENGER AIR BAG AREA DUE TO THE AIR BAG FAILURE. THE CONTACT ALSO MENTIONED THAT THE VEHICLE STALLED DUE TO THE AIR BAG ELECTRICAL SYSTEM. THE CONTACT STATED THAT THE VEHICLE STALLED DUE TO THE AIR BAG ELECTRICAL SYSTEM. THE VEHICLE WAS NOT TAKEN TO A DEALER OR A LOCAL MECHANIC FOR DIAGNOSTIC TESTING. THE APPROXIMATE FAILURE MILEAGE WAS 125,000. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.
THIS COMPLAINT IS SIMILAR TO NHTSA ID NUMBER: 10543085. 08 MERCURY MILAN WITH 3.0L 139,226 MILES STARTED MISSING AND BUCKING WHILE DRIVING 60 MPH ON THE HIGHWAY. TOOK CAR TO THE LOCAL FORD DEALER WHO TOLD ME THAT COIL ON PLUG #4 (COP) WAS MELTED AND HAD FRIED THE VEHICLES PCM. THE FORD DEALER QUOTED ME $2,630.70 FOR THE REPAIR. HE TOLD ME THIS ISSUE WAS COMMON AND KNOWN BY FORD. I CAN SEE HOW A COP CAN GO BAD AFTER 139,226 MILES, BUT I HAVE A HARD TIME WITH A COP MELTING AND SENDING SOME SORT SPARK BACK TO THE PCM AND DESTROYING A $700 PART. TERRIBLE ENGINEERING PRACTICE FORD. IN ORDER FOR THE COP TO MELT TO A POINT SUCH THAT IT DID, IT WOULD HAD TO BE CLOSE TO STARTING AN ENGINE FIRE. THAT WOULD BE VERY BAD INDEED. THIS COULD HAVE EVEN CAUSE A LOSE OF CONTROL AT HIGHWAY SPEEDS. YOU DO THE MATH THE RESULT OF THAT. NOT GOOD. I ALSO FIND IT HARD TO BELIEVE THAT THERE HAS BEEN NO RECALL FOR THIS ISSUE.
CAR ACTED LIKE IT WAS ABOUT TO RUNNING OUT OF GAS. I HAD ABOUT 1/4 TANK OF GAS BUT WENT TO FILL THE TANK IMMEDIATELY. IT STILL ACTED AS IF IT WAS GOING TO STALL OUT, I DROVE VEHICLE HOME AND LEFT IT PARKED IN THE DRIVEWAY. LATER THAT EVENING I WAS TELLING MY HUSBAND ABOUT THE CAR, HE WENT OUT TO TEST DRIVE IT. THE CAR ACTED COMPLETELY FINE. TODAY I WENT TO GO ON A 65 MILE TRIP AND THE CAR STARTED SHAKING ALMOST UNCONTROLLABLY MORE THAN 1/2 WAY WITH A FULL TANK OF GAS. I WAITED TIL I WAS IN A SAFE AREA AND PULLED OVER THINKING THAT MAYBE I DIDN'T WARM THE CAR UP ENOUGH. I SAT FOR SEVERAL MINUTES AND PROCEEDED AHEAD TO MY DESTINATION BUT WAS PETRIFIED THAT I WAS GONNA STALL OUT CAUSE THAT'S HOW THE CAR WAS ACTING. AS SOON AS I ARRIVED I CALLED FORD AND TOLD THEM AND THEY WANTED ME TO WAIT A FEW DAYS FOR AN AVAILABLE APPT. WE TOOK THE CAR TO A LOCAL MECHANIC AND HE MADE US AWARE THAT THE PROBLEM WAS A TBS. THE PCM IS BAD AND COILS ARE MELTED. I WAS JUST WONDERING IF THERE WAS EVER A RECALL ISSUED FOR THIS PROBLEM SINCE I'VE READ SO MANY OF THE SAME COMPLAINTS. *TR
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 26, 2026